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From the Rolls-Royce experimental archive: a quarter of a million communications from Rolls-Royce, 1906 to 1960's. Documents from the Sir Henry Royce Memorial Foundation (SHRMF).
Test report on re-designed 12½% stiffer front springs for a 9-PK car, listing faults and remedies over 10,458 miles.

Identifier  ExFiles\Box 73\3\  scan0268
Date  31th December 1924 guessed
  
SHEET 14.
TEST NO. Xlll.

FIRTHS RE-DESIGNED 12½% STIFFER FRONT SPRINGS - 9-PK CAR.

TROUBLES. | MILEAGE. | CAUSE OR REMEDY.
Main cyl. extra oil pipe broken. | 1259 |
Electrical system failed. | 2361 | Short circuit in switch box - broken wire.
Water in petrol system. | 2611 | Purchased petrol contained water.
A.T. speedometer mileage recorder not functioning. | 27321 | Several teeth stripped off driving pinion of mileage recorder.
N.S. rear brake rope nearly frayed through where it passes through spring support bracket. | 6540 | New brake rope made and fitted.
Inside support bracket for O.S. rear spring king-pin broken. | 7383 |
No.5 big end bearing run. | 9911 | No. 5 piston taken out and test finished on 5 cyls.
Windscreen broken. Front wing stay broken (twice) Front wings continually splitting. | |

MILEAGE OF TEST - 10,458 - AVERAGE SPEED 34.23 m.p.h.

At the end of this test the brakes on this car had completed 31,080 miles.
The work done on them being only - one new rear brake rope fitted and rear brakes re-lined once. Front brake toggle actuating shafts were very loose in their bearings. Also both leading shoe toggle pins were very loose in the brake shoes - the hole in the brake shoes having enlarged considerably.

Hs{Lord Ernest Hives - Chair}/AJL.
  
  


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