Rolls-Royce Archives
         « Prev  Box Series  Next »        

From the Rolls-Royce experimental archive: a quarter of a million communications from Rolls-Royce, 1906 to 1960's. Documents from the Sir Henry Royce Memorial Foundation (SHRMF).
Log of daily tests conducted on an exhaust system, modifying components and measuring performance improvements.

Identifier  ExFiles\Box 14\6\  Scan251
Date  29th October 1931
  
-2-

17.10.31. Cylinder heads and exhaust systems changed back to their respective cars.

18.10.31. Next tests were on 22-EX with Intermediate pipe lagged, Downtake pipe unlagged, and front expansion box unlagged, but reinforced with metal .080" thick round the bottom half (original thickness of box .080")
Result 5% improvement.

20.10.31. Top half of box then reinforced similarly making total thickness of box .160"
Result - 30% improvement.

23.10.31. Whole of expansion box reinforced with a further .080" thickness of metal making total thickness of box .240"
Result - 100% improvement. i.e. as good as standard box lagged.

24.10.31. Downtake pipe re-lagged. This cuts out the swishing noise, and is better than with the pipe unlagged.

25.10.31. Cast Iron expansion box .240" thick fitted.
Result. - as good as standard box lagged.

27.10.31. Lagging removed from downtake pipe and pipe original thickness of .104" reinforced with metal .080" thick making total thickness .184"
Result - 100% - as good as standard downtake pipe lagged.

29.10.31. Lagging removed from Intermediate pipe and pipe original thickness of .064" reinforced with metal .040" thick making total thickness .104"
Result - Better than standard intermediate pipe lagged.

We now have an exhaust system with no lagging which is slightly better than standard made up
  
  


Copyright Sustain 2025, All Rights Reserved.    whatever is rightly done, however humble, is noble
An unhandled error has occurred. Reload 🗙