From the Rolls-Royce experimental archive: a quarter of a million communications from Rolls-Royce, 1906 to 1960's. Documents from the Sir Henry Royce Memorial Foundation (SHRMF).
Proposal to revert to the original method of fixing the spring in the air valve to improve reliability.
Identifier | ExFiles\Box 5\4\ 04-page157 | |
Date | 11th January 1926 | |
STANDARDISATION of CHASSIS PARTS. COMPLETED 22.2.26. Date 11.1.26. X No. 5080 No. 3080 Description of Parts: FIXING OF SPRING IN AIR VALVE. Origin: To improve reliability. Experimental Test Report: It is propose to revert to the original fixing of the spring in the air valve to the top cover by means of a screw. The present arrangement of pushing the top coils into a recess is not reliable. Road Test Report: Fitted to 10-G-111 - run 1200 miles. Fitted to 10-EX - run 800 miles. A similar scheme was fitted to all Silver Ghost cars. Weight of Old Part: Weight of New Part: Difference per Car: Cost of Old Part: £ 1. 4d. 20 HP. £ 1. 10d. 40/50 HP. Cost of New Part: £ 2. 0d. 20 HP. £ 2. 5d. 40/50 HP. Difference per Car: £ 8d. 20 HP. increase. £ 7d. 40/50. Signature of Mr. De LOOZE that above is correct. Hy{Tom Haldenby - Plant Engineer}/Bms. 14.1.26. SIGNATURES, DATE, REMARKS MR. JOHNSON, 22.2.26, Agreed. G.Johnson. MR. B. JOHNSON, 22.2.26, Agreed. B.J. MR. ROYCE, 15.1.26, Agreed. FHR. MR. WORMALD, 11.1.26, Agreed. Wor.{Arthur Wormald - General Works Manager} MR. ROWLEDGE, 11.1.26, Agreed. Rg.{Mr Rowledge} MR. DAY, 13.1.26, Agreed. Da.{Bernard Day - Chassis Design} MR. BAILEY, 12.1.26, Agreed. BY.{R.W. Bailey - Chief Engineer} MR. PLATFORD, 13.1.26, Agreed, as spring clearance does not remain constant, carb. unreliable, advise retrospective action. EP.{G. Eric Platford - Chief Quality Engineer} MR. ELLIOTT, 17/1/26, Agreed OE MR. NORTHEY, 13.1.26, Agreed. PN.{Mr Northey} MR. HIVES, 19.2.26, Agreed. E.Hives. | ||