From the Rolls-Royce experimental archive: a quarter of a million communications from Rolls-Royce, 1906 to 1960's. Documents from the Sir Henry Royce Memorial Foundation (SHRMF).
Continued report discussing brake effectiveness, a burnt exhaust valve, and an incident involving car 35-PK.
Identifier | Morton\M10\ img168 | |
Date | 12th August 1924 | |
contd: -2- of the road and the car was over the bank before the steering could be corrected by the brakes being released. I notice on the previous days reports, you mention that the rear brakes on the car were very effective which we assume relatively would mean that the front brakes were not very effective. We notice on the report of 35-PK car for 12.8.24. that an exhaust valve was found to be burnt. We should like to know what type of valve this was. It is is a Silchrome, please retain it as we should like to examine it. Hs.{Lord Ernest Hives - Chair} | ||