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From the Rolls-Royce experimental archive: a quarter of a million communications from Rolls-Royce, 1906 to 1960's. Documents from the Sir Henry Royce Memorial Foundation (SHRMF).
The results of lagging various exhaust components to reduce tinniness after fitting a new piston.

Identifier  ExFiles\Box 11\4\  04-page080
Date  7th July 1932
  
X7941

To Hs.{Lord Ernest Hives - Chair}
From G.W.H.

Hotel de France,
Chateauroux,
FRANCE.

7.7.32.

19-EX.

We have fitted the new piston and the car has resumed its mileage.

We carried out tests as mentioned in Rm{William Robotham - Chief Engineer}'s memo Hs{Lord Ernest Hives - Chair}/Rm.{William Robotham - Chief Engineer}1/KT.27.6.32. re. tinniness of exhaust system.

(1) The lagging of the downpipe gave no appreciable result.

(2) The lagging of the intermediate pipe gave no appreciable result.

(3) The lagging of the front expansion box gave approx. 50% less tinniness.

We shall try out the combination of the 8 S.W.G. at a later date.

G.W.H.
  
  


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