From the Rolls-Royce experimental archive: a quarter of a million communications from Rolls-Royce, 1906 to 1960's. Documents from the Sir Henry Royce Memorial Foundation (SHRMF).
Tests conducted on a modified exhaust system for the EAC 111.
Identifier | ExFiles\Box 182\M20\M20.2\ img013 | |
Date | 5th April 1924 | |
R.R. 493 (40 H) (SL 42 12-7-23). J.H., D.{John DeLooze - Company Secretary} ORIGINAL EXPERIMENTAL REPORT. COPIES TO: RCJ WOR{Arthur Wormald - General Works Manager} By E.{Mr Elliott - Chief Engineer} Da{Bernard Day - Chassis Design} EP.{G. Eric Platford - Chief Quality Engineer} DN OV. RSJ. Expl. No. 49230 44580 REF. Hs{Lord Ernest Hives - Chair}1/LG5.4.24. TESTER. A.C.Lovsey. Y3H OBJECT OF TEST. To obtain data of exhaust system to be used on EAC 111. CONDITIONS. Standard 40/50 engine on test bench - R.A.F. Indicator. SUMMARY OF TEST. These tests and road tests prove that the modified exhaust system will not cause any appreciable drop in H.P. Further tests are in hand to prove whether exhaust noise has been increased or whether induction roar is manifest. Hs.{Lord Ernest Hives - Chair} | ||