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From the Rolls-Royce experimental archive: a quarter of a million communications from Rolls-Royce, 1906 to 1960's. Documents from the Sir Henry Royce Memorial Foundation (SHRMF).
Replacing K.L.G. sparking plugs due to large gaps causing an engine misfire on B bank.

Identifier  ExFiles\Box 142\3\  scan0187
Date  26th April 1937
  
To Rm.{William Robotham - Chief Engineer}
c. to Rm{William Robotham - Chief Engineer}/Wst.
c. to Rm{William Robotham - Chief Engineer}/FD.{Frank Dodd - Bodies}

1204

Rm{William Robotham - Chief Engineer}/WB.{Mr Brazier/Mr Bell}15/JH.26.4.37.

K.L.G. SPARKING PLUGS.

We have removed the K.L.G. F.30X sparking plugs fitted to 37-EX
The engine was missing fire on B bank (inlet plugs).

Inspection of the plugs showed the trouble to be due to large
gaps .030".

K.L.G. FE.30X have now been fitted.

K.L.G. F.{Mr Friese} 30X have been removed from 33-EX to make way for
K.L.G. F.E.30X.

The F.30X have completed 4223 miles but were serviced after
2914 miles.

Rm{William Robotham - Chief Engineer}/W.Brazier.
  
  


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